Moved blog

| | Comments (0) | TrackBacks (0)
I moved my pantera log to new software. This is one of my excuses for not creating a new entry in awhile. So much to talk about ...

I signed up for the Concorso Italiano. As you all know this event is on August 15th. I hope to have the car in somewhat presentable form but that is looking unlinkely. However, I have gotten to the state where THE CAR MOVED UNDER IT'S OWN POWER! Yes thats right, it moved without anybody pushing it. Matter of fact two weeks ago I drove the car about 10 miles from where I was working on it to my house. The car now sits in my garage.

I installed the driveshafts w/o incident however one of them will rub on the exhaust if the car is on the lift. I'm not very happy about this but the only fix is to heat up the exhaust and bend the pipes to fit correctly. I managed to get the clutch slave installed and adjusted and the brake pedal adjusted properly. I also had to hook up the new brake switch to the brake pedal because the new brake kit doesn't use a pressure sensor.

At this point I should mention that Ken Green from Monterey helped me out for a couple of weekends. He was able to help me diagnose some hazard switch issues and some brake light issues. We found out that the bulbs where not making good contact because of wearing on the solder tips of the bulb. Also the ground at the rear of the car was not that good until we hooked up the ground wire there. We were able to get the automatic cooling fan working but not the manual fan. I have since got the manual fan working as well.

We had to use zip ties to get the throttle cable hooked to the carb because I do not have one of the clips necessary to fit it properly. However I do have a new throttle cable coming from JB. I managed to bolt in the seat belts and the drivers seat. I still had quite abit of wiring hanging about when I took it for the first test drive around the block. The car handled fine. It didn't pull or jump or any wierd stuff, and as far as I know nothing fell off of it. The carb still needs some tuning and probably need to fiddle with the ignition system a bit. But overall we were shocked that everything went so well.

Since then ( two weeks ago ) I have driven maybe 40 miles or so. I have both fans working, and the brake lights, but there is a short in the blinker system that I am having trouble finding. When I put power to the blinker harness the fuse blows. I am also having a body shop look at the scratch in the door to fix that so it is presentable for concorso. At this rate I don't think I will make it. Ther is no trim on the car and I don't have the headlights up yet. Also there are no side windows or door panels, or even carpet. I will just keep working on it and see how far we get for Concorso.

In any case it's been more then three years since I have driven this car. I am still in shock that it is drivable ( I can't believe it ). I am just going to have to keep driving it to get it to sink in!

0 TrackBacks

Listed below are links to blogs that reference this entry: Moved blog.

TrackBack URL for this entry: http://www.grahamjoyce.net/cgi-sys/cgiwrap/brig/managed-mt/mt-tb.cgi/46

Leave a comment

About this Entry

This page contains a single entry by Jason Eaton published on July 29, 2003 9:48 PM.

Starter buttons are cool was the previous entry in this blog.

Moving right along is the next entry in this blog.

Find recent content on the main index or look in the archives to find all content.